G8MNY > TECH 22.04.25 07:45z 215 Lines 10097 Bytes #183 (0) @ WW BID : 30882_GB7CIP Read: GUEST Subj: NORTHERN 650W 2 Stroke Genny Path: ED1ZAC<ED1ZAC<GB7CIP Sent: 250422/0738Z @:GB7CIP.#32.GBR.EURO #:30882 [Caterham Surrey GBR] From: G8MNY@GB7CIP.#32.GBR.EURO To : TECH@WW By G8MNY (Updated Sep 15) (8 Bit ASCII graphics use code page 437 or 850, Terminal Font) I bought this very clean & hardly used non working 63cc one at a junk sale, and "it worked OK last year" I was told! It seems identical to the Wolf, Pro User and KINGAVON versions. On looking into the non-running, there was no intake "suck". This is a 2 stroke with an angled engine and the carburettor ported into the crank case with a reed valve, rather than an upright engine with bottom edge of piston valve intake. Oil Measuring Filler Cap Ü Handle ÜÜÜÜÜÜÜÜÜÜÜ Ú===¿ Û ÞÝ Ú===¿ ÞÝ /~~~~Tank~~~~~\ /~~~~~~Tank~~~~~~~\ ----------------- --------------------- Mains|ÀÄÄÄÄÄÄÄÄÄÄÄÄÄÙÝ DC|~~~~~³~~~~~~~~~~~|On/off |(0)= _-~\ÞÝSilencer |MAINS³ choke []| Choke´Tap Start\\\\\\Plg Ý ³ ø ===== |\ |ÄÄÄÄ¿pull~\\Cyl\ Þ³-----------------| |Pull Air |Carb³,\/~~~\\_-~ Alternatorݳ Air |ø|Start Box &| ³ ³ ( ) ³ ³ß Þ³ Filter | | FilterÀÄÄÄÄÙ\ \___/ / Ý_________________|/ Ú'ÚÄÄÄÄÄÄÄÄÄ¿'¿ ÀÂÄÂÙ ÀÂÄÂÙ """ """ """ """ ENGINE FAULT Checking the ignition, there was a weak spark OK, and there was compression, so I tried putting petrol/ether spray into the crankcase through the reed intake valve, but the engine still did not fire. So I put took the silencer off (needed painting anyway) and put spray through the exhaust port, this did give a bang on turning over, so the ignition and timing was OK. The fault was eventually found to be a popped out crankshaft bearing air seal rubber, between the engine and the alternator. This may have happened if there had been a back fire in the crankcase, or just a lot of compression. There was not usual spring circlip in a groove to hold it in place in this design! ALTERNATOR ± ±SHAFT ± ± TAPERED ±ÝÞ± FIT SHAFTSÞÝÞÝ ADDITIONAL SCREW __ ÛÝÞÛ __ & RIGHT ANGLE ÅÅÄ¿ ÛÝÞÛ ÚÄÅÅÄ SEAL CLAMPS ÄÄÄÄÄÄÅÅ¿³ ÛÛÛÛ ³ÚÅÅÄÄÄÄÄÄ Web Tap³³ ÛÛÛÛ ³³Tap Web hole³°°>ÛÛÛÛ<°°³hole °°> Air tight Oil Seal ³(o)ÛÛÛÛ(o)³ (o) Ball race bearing ÄÄÄÄÄÄÄÄÁ ÛÛÛÛ ÁÄÄÄÄÄÄÄÄ CRANK CASE ÛÛÛÛENGINE INTAKE SUCK ÛÛÛÛSHAFT & TRANSFURE COMPRESSION To get to the fault, I needed to split the alternator off the engine (3 outer bolts) and remove silencer and gently levering off the end casing. A long bolt through the alternator shaft holds it on to the tapered crankshaft, this was the first problem and a smart tap the socket set freed this OK. Then on the lose bolt a sharp tap with a hammer to free the crankshaft off the alternator rotor. Now was the problem of fixing the hardly worn air seal back in place so it would not spin. Initially I used instant gasket sealant, but eventually I added 2 right angle metal pieces, held in by drilled & tapped screws in the available cast lugs around the bearing, these lock the seal in place. But this failed a year later with the captured seal managing to get half way out. I managed to find a new tight fitting seal and a circlip to hold it in place just in cast it started to rotate and loosen as the old one did. ALTERNATOR FAN Also I noticed the Alternator Fan was loose, this removes about 100W of heat, and blows it over the exhaust, but it was able to free wheel! I used 2 part glue (resin and hardener) to fixed that OK, & re-fixed the 2 locating lugs etc. Long Bolt Bearing [~~] [(o)±Þݱ(o)] ±ÞݱSHAFT ÚÂÂÄÂÄÂÄÂÂÄÄÄÄ¿±ÞݱÚÄÄÄÄÂÂÄÂÄÂÄ¿ALTERNATOR ³³³ ³ ³l³³ ³±Þݱ³ ³³l³ ³ ³³³FAN ³³³_³_³u³³_ _ ³±Þݱ³ _ _³³u³_³_³³³ ³g³_glue/±Þݱ\glue_³g³ ²²² ±Þݱ ²²² ÛÛÛÛÛÛÛÛÛÛ±ÞݱÛÛÛÛÛÛÛÛÛÛ ÛÛÛÛÛÛÛÛÛÛ±ÞݱÛÛÛÛÛÛÛÛÛÛROTOR ÛÛÛÛÛÛÛÛÛÛ±ÞݱÛÛÛÛÛÛÛÛÛÛWITH ÛÛÛÛÛÛÛÛÛÛ±ÞݱÛÛÛÛÛÛÛÛÛÛCOIL & ÛÛÛÛÛÛÛÛÛÛ±ÞݱÛÛÛÛÛÛÛÛÛÛDIODE ÛÛÛÛÛÛÛÛÛÛ±ÞݱÛÛÛÛÛÛÛÛÛÛ CIRCUIT Not having the handbook etc. I have reverse engineered the diagram... 12V(20V) 240V AC STOP Charging ÚÄÄÄÄÄ¿ ÚÄo\__ +³ ³- E _³_ bn³ ³bk 3A Bridge N L /// ------------ Rectifier ³ ³ |Electronic|ÄÄÄÄÄÄÄ¿or ³ ³ (155V)³ ³ | Ignition | ³ 7A ³ 15u 450V³ 2.3A | Module | 0R2³2K2 Trip ³ ÚÄ´ÃÄ¿ ³ Trip ------------ ÚÄ()))))ÍÍ» ³ gn³ ³ ye³ ³ ³ ³ ³ ³ ³ ===== º ³gn ³ ³ye ³ ³bk rd³ rd/wh³ bn³ bk³ ³ Coil ºEHT _³_ _³_³ _ _³ _³_ _ _³_ _ _ _ _ _ _ _ _ ³ _ ³_ _ ³_ _ ³ _ _ _ _ ºlead ³ ³ ³ ³ ³ ³ | 34R|( )| ³ ³ º ³0R3³ ³3R2 ³ ³ 6R8 ³ ROTOR | Timing|( )| ³ ³ Plug º À())Ù À((()Ù À(((()Ù Ú(((()¿ | Pickup ÀÄÄÄÁÄÄÄÄÁÂÄÄÄÙ ÚÄ> <5K¼ ==== ==== ===== ³=====³ | & Magneto 730R _³_ _³_ ÃÄ´>ÃÄ´ | /// /// A L T E R N A T O R ÀÄÄRÄÄÙ | C R A N K C A S E ALTERNATOR EXCITATION This is a brushless alternator with the excitation of the rotor magnetically charged up each half cycle from circulating 90ø out of phase currents from the exciting 15uF capacitor. The rotor winding has a diode across (and back emf R) it to maintain the current, half a cycle after the kick. Excitation only starts at high enough RPM (2000RPM) to overcome the diode voltage drop loss, with the weak residual magnetic rotor field. This system is more reliable than the brush type, but it does produce a kink in the load winding waveform and there is no opportunity for voltage control other than engine RPM. CHARGING As I did not have the special DC plug and lead, I made a plug (- |) from 2 brass strips, poked these into socket and through cardboard, to form the plug's mould base, and fitted a cardboard tube. Made the lot into a good mould, and with the petrol tank removed up end the generator to get the socket level, spay oil / grease into the socket holes and refit the plug strips & mould. wires _Þ Ý Mix up resin and hardener with some fiber glass to add strength ÚÅÄÅÄÄÄÅÄ¿ for the plug base. pour in and tamp down. When set remove the new ÀÅÄÅÄÄÄÅÄÙ plug, cut off the cardboard mould, Grind and file off the resin ³ ³ ³ lump into the wanted shape, Solder on the new lead to the brass ³ ³ ³ strips noting +/- and tape the lot up in rubber amalgamating tape, ³_³ ³ this finishes the plug. Although there is a 7A trip (12A to activate!) before the bridge, the rectifier is only made from 4x 3A diodes in the connector box with no heat sink! To improve on this, I cleaned off all the painted copper track, and flowed a thick layer of solder all over it to act as a heat spreader. And I also doubled up on the diodes, putting 4 more on the copper side of the PCB. Note the current trip does not prevent blowing the diodes on wrong battery polarity! So a 13A fuse in the charging lead will help that! In practice though on a good battery the charging current is only 3-4A, but enough to boost a flat car battery (@ 10A ?) in a few mins so you can crank the car over. OTHER MODIFICATIONS 1/ To reduce the VHF/UHF ignition noise, I have added a loose coax braid over the lead earthed at the plug screened cap. ________ Added loose Coax Braid Metal ³ÜÜÜÜÜÜÜ-================================----- EHT Lead To Cover ³Ý|n|ÜÜÜ-================================ÄÄÄÄÄ Magneto coil suppressor ³Ý³~³Þ|~~~ plug cover³ÚÙ À¿³ _ ³³~~~³³ CylinerÁÄÁÄÄÅÄÄÄÅÄÄÄ À~u~ÙSpark Plug 2/ To improve the voltage regulation, I applied my current solenoid feed forward modification. This was easily done, by adding a small solenoid (e.g. from an old VCR) rewound with a few turns of suitably insulated & thick enamelled copper wire, that takes the 230V 4A full load current (neutral). Mounted is with a single large screw, firmly on the engine webbing, by the speed setting adjuster. (Tap/Make hole in webbing) The solenoid piston is linked up to aid the speed setting spring as the load comes on. The length of the thick link wire is critical so that the piston only just goes fully home at full throttle, and if less compensation is needed the wire can be bent slightly to adjust the effect (Mount the petrol tank via a pipe elsewhere for testing). __ CRANKCASE BOB ³()³AXLE WEIGHT GOVERNOR³ ³ ³ ³ SPRING ___ SPEED ³ o³ÄÄÄ,/\/\/\.ÄÄÄÄ[___[ADJUSTOR SCREW ³ o³ Link Wire ÚÄÄÄÄÄÄÄÄ¿ ³ o³============²²³SOLENOID³ ³ ³ BOOST__\ ÀÄÄÄÄÂÄÂÄÙ Alternator ³ ³ PULL / bk³ ³bk Load ³ ³ Neutral Neutral ³ o³_________ ÀÄÄÙ Throttle link N.B. Solenoid pull is proportional to:- 1/ the Mains load current squared, 2/ the number of turns on solenoid coil, 3/ the location of the movable iron piston slug. With this modification a good 230V @ 750W peak is available under resistive lamp load tests from this small generator. CONCLUSION Although 2 stokes are not the best engine for efficiency etc. and fuel oil mix is needed, their simplicity and reliability if maintained (clean carburettor and muffler) it does give a simple lightweight power source. The noise of this one changes from poor putting misfires on no load, to a steady 50Hz hum on higher loads. N.B. if the engine is difficult to start, "ether spray" in the air inlet does help! So a lot of work was needed, but now I have good genny in the end for /P work. See my TECH buls "Regulating 12V Generator Output", "Cheaper Generators" & "Petrol Generators for /P SSB" Y Don't U send an interesting bul? 73 de John G8MNY @ GB7CIP
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